Some SdKfz 222 Upgrades
Posted: Fri May 14, 2021 7:00 am
After talking with some fellow collectors on the weekend there seems to be the impression that the forum has lost a bit of its zip since Phil is no long entertaining use with his fabulous skill, not at all degrading the standard build from the plans in anyway, but it is that spark of imagination that can come from seeing someone else’s creativity that can really add to the enthusiasm and give you a little kick to keep the interest alive. So I thought that I might add some of the upgrades that I have done to my SdKfz222 over the past year or 2 (time is starting to go too fast) definitely not in the quality of some of the other posts but it might spark some imagination.
As our quality inspector at work would say these are not criticisms but improvement opportunities. I will try not to offend any initial design work done, but there is a lot of room for improvement that will make this an exception model. Bodo did a beautiful job with his adding and improving the overall look, far better than I could do, but I wanted to make it a more useable model something that I could drive anywhere.
Looking at the drive system it became obvious that the centres of the axle shaft joins where in the wrong positions the diff join too far away from the chassis rail and the wheel joint too close to the chassis. Also the hole through the chassis was a little too small. This caused the drive shaft to lock on full bump or droop, or prevented suspension movement when on full lock. To fix this issue I found some off the shelve drive shafts that would fit and machined some extensions for the diff housing so the inner join was closer to the chassis. I then increased the size of the hole in the chassis to the maximum. Then I machined up some new outer axle hub shafts to get the outer joint closer to the kingpin centre line. This then require a new wheel mounting hub and as I was making the new wheels this wasn’t an issue (the new wheels will fit the original hubs). Unfortunately I could not improve the scrub radius but on the real thing this was quite large anyway.
The new shafts now gave plenty of travel and the opportunity to improve the steering angles which I though where a little low. So after grinding the corners off the lower swing arm the steering arm could move further inward I then redesigned the steering arm with more of a curvature to reach around the lower control arm and full droop.
While I was working on the steering I thought that I might have a go at improving the linkages, with the hope to get the 2 wheel – 4 wheel steering to work. Based on as much information as I could find I estimated that the rear wheels did not turn as far as the front (I may be completely on the piss on this) so into the CAD for a day or 2 and I ended up with what I think is the right Achermann for the 4 wheel steering that still fits with the 2 wheel steering. Not that any of this really matters on this scale but nice to have it as right as I can.
During all of this I noticed that the diffs where only fitted with a single bearing on the pinion, being a rather heavy model I thought that this should be rectified. So a bit more laser cutting and machining and I ended up with a bracket that did both, fix the steering linkages and held in place a second pinion bearing.
With the steering sorted I was back to the bump and droop, I was not a fan of the through bolt bump stops and hoped that I would eventually put Shock absorbers on that could do that job but until then I need something else. So a small laser cut plate bolted to the original bolts did the job. While I was here I looked at adding some camber adjustment on the upper control arm mount. After consideration of the effect the new bump stop will have (putting considerable bending load) on the chassis mount for the upper control arm and the fact that I have just made the mount weaker by the slots I put a 3mm support plate on top of the mount. (picture above) I also added smaller 3mm support plates to the bottom control arm lower mounts, at the area where that chassis rail acts as the bump stop for full bump.
So now with the control arms mounted to the chassis I looked at the kingpin and hub arrangements, my kit didn’t get the upgrade to the steel bearing housings so every thread in the aluminium housings was fitted with a recoil/helicoil to make sure that things stayed put. Which brings me to another issue and that is loctite which is good stuff in the right place but no substitute for the correct bolt tension on a good design. So back to the lathe to make some bushes for the pivot bolts that hold the kingpin housing. Using a simple tube bush so that the bolt can be tightened to a correct tension without loading/locking onto the arm worked a treat. Along time ago an old bloke said to me “if it needs to move to do its job than make sure it can move as free as you can make it move”, and I apply that to every moving part.
Then all I had to do was the steering from the servos, yes I chickened out on the mechanical change linkage as is on the real machine and went for the easy 2 servo option. It made for the 2-4 wheel change over easier in the program on the controller and is locked to the gear select.
As our quality inspector at work would say these are not criticisms but improvement opportunities. I will try not to offend any initial design work done, but there is a lot of room for improvement that will make this an exception model. Bodo did a beautiful job with his adding and improving the overall look, far better than I could do, but I wanted to make it a more useable model something that I could drive anywhere.
Looking at the drive system it became obvious that the centres of the axle shaft joins where in the wrong positions the diff join too far away from the chassis rail and the wheel joint too close to the chassis. Also the hole through the chassis was a little too small. This caused the drive shaft to lock on full bump or droop, or prevented suspension movement when on full lock. To fix this issue I found some off the shelve drive shafts that would fit and machined some extensions for the diff housing so the inner join was closer to the chassis. I then increased the size of the hole in the chassis to the maximum. Then I machined up some new outer axle hub shafts to get the outer joint closer to the kingpin centre line. This then require a new wheel mounting hub and as I was making the new wheels this wasn’t an issue (the new wheels will fit the original hubs). Unfortunately I could not improve the scrub radius but on the real thing this was quite large anyway.
The new shafts now gave plenty of travel and the opportunity to improve the steering angles which I though where a little low. So after grinding the corners off the lower swing arm the steering arm could move further inward I then redesigned the steering arm with more of a curvature to reach around the lower control arm and full droop.
While I was working on the steering I thought that I might have a go at improving the linkages, with the hope to get the 2 wheel – 4 wheel steering to work. Based on as much information as I could find I estimated that the rear wheels did not turn as far as the front (I may be completely on the piss on this) so into the CAD for a day or 2 and I ended up with what I think is the right Achermann for the 4 wheel steering that still fits with the 2 wheel steering. Not that any of this really matters on this scale but nice to have it as right as I can.
During all of this I noticed that the diffs where only fitted with a single bearing on the pinion, being a rather heavy model I thought that this should be rectified. So a bit more laser cutting and machining and I ended up with a bracket that did both, fix the steering linkages and held in place a second pinion bearing.
With the steering sorted I was back to the bump and droop, I was not a fan of the through bolt bump stops and hoped that I would eventually put Shock absorbers on that could do that job but until then I need something else. So a small laser cut plate bolted to the original bolts did the job. While I was here I looked at adding some camber adjustment on the upper control arm mount. After consideration of the effect the new bump stop will have (putting considerable bending load) on the chassis mount for the upper control arm and the fact that I have just made the mount weaker by the slots I put a 3mm support plate on top of the mount. (picture above) I also added smaller 3mm support plates to the bottom control arm lower mounts, at the area where that chassis rail acts as the bump stop for full bump.
So now with the control arms mounted to the chassis I looked at the kingpin and hub arrangements, my kit didn’t get the upgrade to the steel bearing housings so every thread in the aluminium housings was fitted with a recoil/helicoil to make sure that things stayed put. Which brings me to another issue and that is loctite which is good stuff in the right place but no substitute for the correct bolt tension on a good design. So back to the lathe to make some bushes for the pivot bolts that hold the kingpin housing. Using a simple tube bush so that the bolt can be tightened to a correct tension without loading/locking onto the arm worked a treat. Along time ago an old bloke said to me “if it needs to move to do its job than make sure it can move as free as you can make it move”, and I apply that to every moving part.
Then all I had to do was the steering from the servos, yes I chickened out on the mechanical change linkage as is on the real machine and went for the easy 2 servo option. It made for the 2-4 wheel change over easier in the program on the controller and is locked to the gear select.